Before I begin, I would like to express my respect for technicians. They have a difficult job and many are highly skilled and reliable. However, as an inspector, I have noticed that technicians far too often rely on technology and past experiences rather than the basic fundamentals of diagnostics. The actual problem can be overlooked due to technicians depending on high tech equipment and the multitude of modules that are standard in most of today’s vehicles. Starting with step one – doing an overall check of the vehicle - seems too simplistic and is often bypassed, even though it takes very little time and usually does not require specialized tools or equipment. Therefore, an inspector should never assume the basics have been checked. Although it is not an inspector’s job to diagnose the problem, taking the time to do so can sometimes reveal the actual cause of failure or a potential pending failure. Below, I have chronicled times when this has occurred in my own personal experiences.
The technician claimed a vehicle’s overheating was caused by no coolant flow in the radiator due to a failed water pump impeller very rare. The actual problem was caused by a worn radiator cap that was not pressure tested.
The technician claimed the failure of a front wheel bearing was due to excessive play at the wheel. The wheel was very loose. The C/V axle nut did not appear to be threaded all the way on to the shaft. After asking the technician to tighten the loose nut, the play was eliminated.
When inspecting a diesel with a supposed fan clutch failure and a code of “circuit failure/no communication,” I found the problem to be a severed harness at the connector caused by, none other than the fan itself! The technician never checked the connector!
The technician claimed that no voltage to the alternator was due to failure to the harness. He came to this conclusion because “they see it all the time.” Failure was actually due to a very loose battery cable end at the battery. The technician actually thanked me for discovering the loose cable because he was not looking forward to replacing the harness.
The technician claimed that all TPMS sensors had failed because they all had codes and would not reset. The vehicle was a ¾ ton truck with new tires that required 78 psi in the front and 55 psi at the rear, as stated on the tire placard. All four tires had 45 psi. After inflating the tires to the proper pressure the warning light turned off.
After replacing the left rear folding seat back motor on a van, a technician found that the right side would not raise properly, even though it had been working when he lowered it. Therefore, he claimed it also needed a new motor. The failure was actually caused by the headrest binding on the front seat back because the technician had not removed the headrest before lowering the seat.










